






The king of the screwdrivers strikes again

Keeps me busy that barsteward

Should have been the first thing you checked pimp, Its the first thing i check with dodgy displaysbigpimp347 wrote:
so after all that is was probably just the resister,
bigpimp347 wrote:i've just spent nearly three hours getting a channel LED to work in a uniden 200..!!
one bar out, simple...change the display as it's normally a dry joint or display..
nope, changed it, nothing still out.
check all circuits, all ok, no broken tracks..
try another LED.. nope..
change the selector (just in case) nope..!!
so check all resisters....BINGO, last one i check has gone..
change it, drip a bit of snot on the selector (got a bad cold)
power it up, a different segment out and some dodgy ones barely lit..
so i try again, clean it up and still one out and some dodgy ones..
then nothing...damn ribbon snapped, re do the ribbon, bingo, all seem ok, oh hold on some dodgy ones..
re solder the channel selector, hear the snot sizzling..ah haa..!!
switch cleaner and heat gets rid of the snot..
then...no display, again..
the ribbon went again.. feck me...then it works and...another bar out..
so some IDE hard drive ribbon out the drawer, re cut and soldered, all lights up and ready to go..
all this for a tenner..!!
so after all that is was probably just the resister, but age and the ribbon keep going didn't help..!!
now all tuned up and ready to go back, next in line will be a york 863 80ch (no locking right) and an old grandstand homebase to service..!!
right i'm off to bed, busy day tomorrow..!!
PLL02A wrote:Should have been the first thing you checked pimp, Its the first thing i check with dodgy displaysbigpimp347 wrote:
so after all that is was probably just the resister,
PLL02A wrote:Had a harrier CBX in for repairs today, First job was to change the L.E.D display as a few of the digits were out, I soon found out why, Someone had changed it at some point and it looked like it had been soldered with a flame thrower![]()
Next job was to undo a dodgy squelch mod, A 10k resistor had been replaced with a 160k one
Wasnt even making contact as they had ripped the track off it
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Next job was to find out why the channels were arse for elbow, Which turned out to be broken pins on the channel selector, Who ever changed the ch display had obviously broke them
Another 80s classic saved
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The king of the screwdrivers strikes again
Keeps me busy that barsteward
Cant beat the old skool rigsBigdave wrote:
Glad you saved a classic m8 had one backin the day not a problem with it ever....................
Nice work, Another old classic saved from the binLaw_Sayer wrote: ↑14 May 2022, 01:40 Update.
It's working VCO was indeed outBuick
was giving me 2v on receive and 3.1v on TX now they set to 4v each also as suspected nasty solder work had to retrace 4 tracks that had been burned/ lifted
. Swiped a couple of ferrit cores from the CB-X mobile to fix the broken ones in the CB-HQ as the CB-X has bad necrosis no real loss , spares for another time.